Portable Biogas Microturbine Power System Installation



Similar documents
Capstone C330 Microturbine Operation in Alberta s Oilfields. Presented by Dan Boonstra January 17 th 18 th 2002 DOE / CETC / CANDRA Conference

C60 CUMMINS/CAPSTONE CHP WITH REMOTE DISPATCH

Micro cogeneration. Affordable, efficient and innovative

Medical Air Systems: Scroll

THE EUROPEAN GREEN BUILDING PROGRAMME. Technical Module on Combined Heat and Power

CPX/HT Series. REFRIGERATED AND HIGH TEMPERATURE DRYER 12 to 2400 CFM. High-performance products. Designed for you!

CNG, LNG, and Other Fuels from Landfill Gas ---Prospects for Future Development----

Drives and motors. A guide to using variable-speed drives and motors in data centres

Micro-Turbine Combined Heat & Power Generators (CHP) Cold Climate Applications 2014 Polar Technology Conference Richard S.

October 8, WHP Waste Heat-to-Power Fuel and Emission Free Power

Current state of plant Functioning as a peak and emergency centre. Statistics Accumulated operating hours:

Drives and motors. A guide to using variable speed drives and motors in data centres Meeting your Carbon Reduction Commitment (CRC)

BIOENERGIA DE NUEVO LÉON, S.A. DE C.V.

Screw Compressors 11-22kW

PacifiCorp Original Sheet No. 476 FERC Electric Tariff, Substitute 6 th Rev Volume No. 11 APPENDIX 2 TO SGIP

MEDICAL AIR STATIONS FOR MEDICAL GAS PIPING SYSTEM. Key features: NOVAIR quality and service:

Refrigeration & Air Conditioning

Electrical Engineering

ThermoSorb Desiccant Dryers

Federal Wage System Job Grading Standards for Air Conditioning Equipment Operating, Table of Contents

KU DESIGN GUIDELINES APPENDIX XVI RECOMMENDED BAS I/O CONTROL POINTS BY EQUIPMENT / SYSTEM

The State Fire Marshal's Office and the VDH/Office of Licensure and Certification. Generator Testing in Nursing Facilities

ETC -SV. Class 0 oil-free compressed air through catalysis

MAINTENANCE INSTRUCTIONS. Thermia Robust heat pump

Ship Propulsion/Electric Power Hybrid System Recovering Waste Heat of Marine Diesel Engine

FULL ELECTRICAL LNG PLANTS: HIGHEST AVAILABILITY AND ENERGY EFFICIENCY THROUGH OVERALL SYSTEM DESIGN

CRITICAL COOLING FOR DATA CENTERS

Rotary screw compressors kw 5,5 7, , bar MODULO

Direct Fresh Air Free Cooling of Data Centres

Natural gas liquids recovery from gas turbine fuel

Example Retrocommissioning Measure: Opening Throttled Discharge Valves

TECHNICAL SPECIFICATION. StirLIN-1 Economy Liquid Nitrogen System

ROTARY SCREW COMPRESSOR. RMD kw

INSPECTION AND TESTING OF EMERGENCY GENERATORS

SIX REASONS TO DRY BIOGAS To A LOW DEWPOINT BEFORE COMBUSTION IN A CHP ENGINE STEVEN SCOTT MARKET DEVELOPMENT MANAGER ALTERNATIVE ENERGIES

Chris Clement 701 Bayou Lane Thibodaux, LA

Inverter and programmable controls in heat pump applications

Maintenance for Energy Efficiency

Heat Recovery and Compressed Air Systems

Diesel Generating Set

Best Practice Guide BPGCS007

DEMONSTRATION OF COMBINED HEAT AND POWER TECHNOLOGY AT A DATA CENTER

Commissioning - Construction Documents (Page 1 of 6)

Statement of Work. 3.0 Details of Service Pre Start-up Cooling Start-up Service. Installation Service. Table of Contents. 1.0 Executive Summary

Microsoft - Cheyenne Board of Public Utilities Biogas CHP Demonstration Project

Diesel Engine Driven Generators Page 1 of 6

Backup Fuel Oil System Decommissioning & Restoration Plan

UTILITIES DEPARTMENT NORTH CAMPUS DISASTER RECOVERY PLAN

Printing and Publishing Energy Savings Guide

Source: EIA Natural Gas Issues and Trends 1998

Xcel Business Customers: Program and Rebate Summary

INDUSTRIAL DIRECT DRIVEN PISTON COMPRESSORS CL - CH - CK

Unit 1 Turbine Rotor 110 MW Replacement

hybrid fuel cell bus

Refrigeration & Air-conditioning Technician

USING KPI S FOR PEAK EFFICIENCY

Mechanical Engineering Technician- Plant Technician

LG Electronics AE Company, Commercial Air Conditioning

Top Technology for Industry, Agriculture, Business and Communities

14. Troubleshooting Guide

Commercial Gas Heat Pump - VRF

Tour of new eircom Data Centre Blanchardstown by Dervan Engineering Consultants 11 th March 2015

Indoor coil is too warm in cooling mode or too cold in heating mode. Reversing valve or coil thermistor is faulty

Nirvana. Cycling Refrigerated Dryers

SCADA Controlled Multi-Step Automatic Controlled Capacitor Banks & Filter Banks

Presentation Outline. Common Terms / Concepts HVAC Building Blocks. Links. Plant Level Building Blocks. Air Distribution Building Blocks

ORC TURBOGENERATOR TYPE CHP - Organic Rankine Cycle Turbogenerator fed by thermal oil, for the combined production of electric energy and heat -

Expansion Pitfalls, Permitting and Compliance A Case Study

Half the cost Half the carbon

Planned and Emergency Utility Outage Guidelines

HR Heated HB Blower. Smart Solutions for Drying Compressed Air. Dual Tower Heat Reactivated Desiccant Air Dryer

AGENDA STAFF REPORT. Budgeted: Yes Current Year Cost: $695,000 Annual Cost: N/A

Ground-breaking conversion of critical Data Room WaterChiller from R22 to R422D / MO29

David Mezzacappa, P.E. SCS Engineers Contractor to U.S. EPA on LMOP

ENERGY MANAGEMENT. for INDUSTRY AND BUSINESS

Technical Specification. Generating Set with Waukesha engine burning natural gas

products 22 º C Ventilation Air Conditioning Refrigeration Energy & Cost Saving Products Inside PROVIDED BY HEINEN & HOPMAN

PREVENTIVE MAINTENANCE PROGRAM AND NOVEL TECHNIQUES TO REDUCE DOWNTIME AND INCREASE OPERATING EFFICIENCY AT DISTRIBUTED COGENERATION FACILITIES

ECOCIAT. Domestic hot water heat recovery unit

T-100-R Installation Guide

technical data air conditioning systems RXS E (single phase) FBQ-B8V1-B8V3B Split Heat Pump Condensing Units Split Sky Air

GLOBACON 05 HVAC Systems for Cogen

THERMO KING TRUCK & TRAILER UNIT ALARM CODES THIS DOCUMENT SHOWS ALL CURRENT ALARM CODES FOR THERMO KING TRUCK AND TRAILER UNITS.

Energy Storage Activities at New York Power Authority

LG Air Conditioning Multi F(DX) Fault Codes Sheet. Multi Split Units

Design and Test Operation Performance of 1,500 C Class Gas Turbine Combined-Cycle Power Plant:

Structure of this presentation

Elements Elements describe the essential outcomes.

NEXGEN Cloud Cloud Software Services and Hosting for NEXGEN Smart Meters

Data Realty Colocation Data Center Ignition Park, South Bend, IN. Owner: Data Realty Engineer: ESD Architect: BSA LifeStructures

HEATER, AIR CONDITIONING AND VENTILATION

HP switch LP switch Discharge thermo Comp. Surface thermo


Design Guide. Retrofitting Options For HVAC Systems In Live Performance Venues

Facilities Maintenance Standards rev

Screw Compressors ESM Fixed Speed & VS Variable Speed

Failure code manual. content

Designed for multi-injector endurance testing, the

Cat Electronic Technician 2015A v1.0 Product Status Report 4/20/2016 2:49 PM

Transcription:

Portable Biogas Microturbine Power System Installation CANMET Energy Technology Centre & The City of Calgary Chuck Smith, P.Eng. CH2M HILL chuck.smith@ch2m.com 5th Annual Microturbine Applications Workshop January 25-27, 2005, Ottawa, ON

Project Organization Funding & Project Support CETC (75%): Microturbine Trailer Operations The City of Calgary (25%): LFG Recovery, Supply & Monitoring Project Management CH2M HILL

Installation Summary Location: Shepard Landfill, Calgary, AB Portable Unit: Trailer-mounted Capstone C30 complete with on-board LFG conditioning system Unit initially tested in 2001 (1,051 hours); Re-installed November 2003 with LFG conditioning system upgrades; Operated to November 2004 (6,202 hours)

Installation Summary Grid interconnected installation Trailer sited on top of completed landfill waste cell; 25kV feeder brought to unit CompAir Hydrovane 15 hp compressor used to draw LFG under vacuum from dedicated LFG extraction wells on site LFG flow rate ~ 22 m 3 /h for 30 kw Capstone C30 microturbine

Site Installation 25 kv Interconnection Point Microturbine Trailer LFG Extraction Well (TYP) Abovegrade Gas Lines (3 LFG Wells connected)

Project Goals Obtain at least 6 months or 4,000 hours of operational experience Unattended operation with Web-based monitoring system Site visits for routine O&M to be on a monthly basis

Unit Equipment Summary Gas processing system Inlet filtration - coalescing filter VanAir deliquescent gas dryer low pressure (Model D-30) Comp Air Hydrovane Model GK707 rotary vane 15 hp compressor direct-coupled dual-circuit aerial cooler for gas and lube oil cooling Compressor control panel

Unit Equipment Summary High pressure water knock-out vessel Gas/glycol heat exchanger (plate type) for optional gas chilling system Gas/gas heat exchanger (plate type), to re-heat the gas ~ 10 C above dewpoint AFT SAG-18 siloxane filtration system Automated condensate handling system

CompAir Hydrovane GK707 Compressor Gas Aftercooler AFT-SAG-18 Siloxane Filter Condensate K.O. Gas/Glycol Heat Exchanger (optional Chilling Loop available)

Unit Equipment Summary Power generation system Capstone 30 kw microturbine Unifin Microgen Heat Recovery unit DY600 heat-driven adsorption chiller initially installed and tested for gas chilling application; removed due to limitations of the DY unit capacity and system component failures Electrical room (power output 480V or 600V) Net-Flow Web-based monitoring system

Unifin MicroGen HRU Manual Exhaust Diverter Valve Low Voltage Visible/Fused Disconnect Import/Export Meter Capstone C30 DY600 Chiller Trailer Electrical Panel

Electrical Single Line Diagram

LFG Conditioning System Performance LFG conditioning system operated as designed; only minor maintenance issues Downtime associated with fuel gas system: Condensate dump valve malfunction on air delivery side (two separate occasions) Fuel gas PCV upstream of microturbine not seating properly. Deposits found on valve seat Total Siloxanes measured: Raw LFG from the wellfield: Treated LFG to Microturbine: 5.13 ug/l 0.05 ug/l

Electrical Performance Operation Interval April 3 November 13, 2004 Max. Turbine Output (kwe) 30 Min. Turbine Output (kwe) 25 Average Power Output (kwe) 27 Total Estimated Power Generated during interval (kwh) 111,000 Total Microturbine Online Hours 4,425 Total Power Exported to Grid (kwh) 83,067 Total Power Imported from Grid (kwh) 1,278 Average Net Power Output to Grid (kw) 20 Average Parasitic Power (kw) (compressor, pumps, fans, lighting, etc.) 7 Average Onsite Parasitic Power (as a % of total) 25% System Online Availability during interval 84%

O&M Performance Availability Nov. 2003 - Nov. 2004 = 59% Delays in DY600 installation/modifications DPC failure and delays in repair (1,428 hours) Microturbine generator shaft failure (1,527 hours) Availability Apr. 2004 - Nov. 2004 = 84% Projected annual O&M costs = $28,000 Microturbine and HRU ~ 3.7 cents/kwh Gas Conditioning System ~ 9.0 cents/kwh Above costs based on quarterly inspection for the microturbine and PM on gas compressor

Capstone C30 On-line Output April - November 2004 70.00 Power (KWe) 60.00 50.00 40.00 30.00 Web-Based Monitoring System Operational Average Power output Fuel Fault ESD Valve (Low N2 Pressure on ESD Valve - FC) DY600 Chiller Testing (May 20 to June 8) Fuel Conditioning System Maintenance Remove DY600 System Offline Compressor Service + Oil Change (4550 hrs) Fuel Pressure Fault To MT Decommission MT Trailer System Nov 17-20 Planned ENMAX Outage Fast Undervolt Phase C INVDSP Bus Over Voltage 20.00 10.00 Fuel Fault ESD Valve (low N2 Pressure on ESD Valve - FC) Finish Test Phase 0.00 06/05/2004 05/15/2004 04/24/2004 04/03/2004 06/26/2004 07/17/2004 10/09/2004 09/18/2004 08/28/2004 08/07/2004 11/20/2004 10/30/2004 Date

Web-Based Monitoring Last Poll: 03-11-2004 17:57:08 CETC MICROTURBINE TRAILER - SHEPARD LANDFILL, CALGARY, AB Process Information Gas Temperatures Phase A Power Average 10 kw Heat Exchange Temperature 1 22.7 C Phase B Power Average 9.88 kw Heat Exchange Temperature 2 22.5 C Phase C Power Average 10.04 kw Heat Exchange Temperature 3 50.76 C Power Output 30.11 kw Heat Exchange Temperature 4 32.65 C Phase A Current 33.9 A Heat Exchange Temperature 5 0 C Phase B Current 33.99 A Heat Exchange Temperature 6 0 C Phase C Current 33.99 A Heat Exchange Temperature 7 0 C Neutral Current 0 A Heat Exchange Temperature 8 0 C Total Phase Current 101.5 A Other Temperatures Phase A Output Voltage 289.82 V MicroTurbine Room Temperature 6.31 C Phase B Output Voltage 288.56 V Compressor Room Temperature 4.94 C Phase C Output Voltage 290.34 V Outside Ambient Temperature 4.81 C Frequency 60.21 DY Chiller Parameters Supply Voltage 13.94 V Energy Flow Rate 1-1.29 MJ/hour Ambient Pressure 89 kpa Cooler Temperature 1 27.75 C Exhaust Temperature 11.02 C Energy Flow Rate 2-1.28 MJ/hour Engine Speed 95744 RPM Cooler Temperature 2 27.75 C Exhaust Temperature 579.36 C Export Power Meter Run Time 5979 Hrs Power Plus 0 kw Microturbine Alarm Status Power Minus 0 kw RPM Alarm Status Power Plus Var 0 kvar CO Alarm Status Power Minus Var 0kVar DY-Chiller Alarm Status - Currently Offline Landfill Gas Parameters Flow Rate 20.5 m3/h Methane 58.5 % Oxygen 0.35 %

System Component Failures Major DPC components failure (1,428 hours) IPM Module burn-out Pre-charge board Phase C resistor Inverter IGBT open Microturbine shaft failure (1,527 hours) Minor Gas Compressor - motor coupling failure (4,550 hours)

General Experience Areas for Improvement Reduce O&M costs through local mechanical service company and trained local technician Future Market Opportunities Smaller remote landfill sites, or small-scale digester gas operations Development / R&D Opportunities Field testing new micro-power generation systems - e.g. Stirling engines

Overall Experience After replacement of microturbine hot-section, the system operated at over 80% on-line availability; down-time associated with grid faults and fuel faults Adjustments in protective relay settings and with fuel delivery system maintenance, on-line availability increased to over 90% High projected O&M costs associated with biogas compression and treatment, resulting from: Lack of local service Oversized capacity for future power generation Web-based system effective for system monitoring and data storage